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cleaner production case study
 

Tony's Tuna International

Summary

Traditional approach

Cleaner production initiatives

Benefits

Where to find additional information

 

January 2001

Summary

A detailed investigation into water usage and wastewater generation at Tony's Tuna International, which produces sashimi tuna primarily for the Japanese market, identified possible improvements in both quality and quantity, particularly in the washdown and pilchard thawing areas. As a result of this consultancy and changes in its practices the company has reduced annual water usage significantly and saved $24,874 in 2000 on pilchard thawing alone.

Business Profile
Tony's Tuna International (TTI) is a major tuna processing company based in Port Lincoln that produces sashimi tuna primarily for the Japanese market. It is one of the most modern tuna processing plants operating in Port Lincoln, having undergone major upgrades in the past five years. The tuna industry currently dominates aquaculture in South Australia and has an economic value of over $500 million.

Financial assistance provided
Flinders University of South Australia carried out the consultancy with a grant of $15,000 from the SA EPA and funding through the Coast and Clean Seas scheme. The consultancy covered eight major processing facilities in Port Lincoln.

Technology implemented
A detailed investigation of water usage and wastewater generation (both quality and quantity) identified areas where major savings could be made, particularly in washdown and pilchard thawing. An investigation into the optimum regime for temperature exchange during pilchard thawing showed that significant savings could be made by changing the water inlet to the base of the thaw-out bins and by pulsing water exchange via solenoid valves. Australian Quarantine Inspection Service requirements are maintained through the use of backflow prevention valves on the main inlet pipe.

Cleaner production motivators
Waste minimisation was considered important for continuing economic operation of the facility, and the Coast and Clean Seas project was an important driver for the study.

Traditional approach

During the period March 1999 to March 2000, TTI used 26,877 kL of mains water, mostly for pilchard thaw-out. The traditional approach to pilchard thawing was to defrost pilchards using cold water in open tanks with water running continuously. This approach was inefficient and required more than 12 kilolitres of water per tonne of pilchards. Traditional washdown practices also used water inefficiently and wastefully.

Cleaner production initiatives

Pilchard
Pilchard thaw-out
Pilchard thaw-out

Benefits recommended and implemented
Pilchard thaw-out process improvement
The process used for pilchard thaw-out was improved significantly and water usage has decreased from more than 12 kilolitres to approximately 3.73—5.6 kilolitres per tonne, depending on mains water temperature, with no increase in processing time.

Monitoring
A thorough review of all on-site water usage and wastewater generation was instigated in the program, identifying opportunities for minimisation. Use of water for sashimi tuna processing is low, but possible additional savings during washdown have been identified and further changes in operational procedures should save more water and improve ongoing waste treatment charges in the future. The activities identified for continuing savings in water usage include cleaning freezer rooms, harvest bins, pilchard thaw bins, vehicles and net cleaning. Hosing down after scrubbing with cleaning agents is now done through flow regulated nozzles.

Benefits

Environmental  
Water usage
  • A reduction from >12 kL to 3.37—5.6 kL/t in water for the thawing of pilchards.
Waste reduction
  • Reductions in nutrient load in wastewater will have significant benefits for the re-use of wastewater treatment plant effluent being implemented in the Coast and Clean Seas initiative.
Economic  
Productivity
  • Productivity and cost efficiency have increased significantly as a result of changes implemented.
Water usage costs
  • Water usage has decreased, resulting in direct savings in excess of $24,000 per annum for pilchard thawing alone.
Future waste treatment costs
  • Future trade waste discharge fees to sewer will be based on both volume and strength; savings in charges through waste minimisation, separation of high nutrient streams, use of screens etc. will result in significant future savings.
Payback period
  • Costs associated with the new pilchard thawing system are low, totalling <$ 1000 for new piping, solenoid valves, bin adaptations.
  • Payback period for measures aimed directly at waste minimisation is estimated to be less than one month.

Where to find additional information

Eco-efficiency Team
Environment Protection Authority
GPO Box 2607
Adelaide SA 5001

Phone: (+61 8) 8204 2004
www.epa.sa.gov.au

Mr Trampas Culter
Plant Manager
Tony's Tuna International
Pine Freezer Road
Port Lincoln SA 5606

Phone: (+61 8) 8682 2266

This page was last modified 14-08-2007
 

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